COLD SANDWICHES AND GENERATORS
By Larry Bush

- Ref: generator sets, power generation equipment, emergency
generator, emergency power, power equipment
Summary:
"A story about keeping emergency power
generator sets running against all odds."
As Foreman of the emergency generator unit for community services areas
in the Saudi Arabian Oil Company, I was always on the lookout for
additional generator sets. The unit needed a spare generator set around
1000 KW to use as a temporary replacement for out of service generator
sets.
My co-worker, Abdullah and I had been directed to an unused generator
set that had supplied emergency power to a Company owned and maintained
worker accommodation camp for Company employees. The Company shut the camp
down four years earlier.
The camp was currently being used by a Company sub-contractor and the
generator was not in use. Pigeons had apparently used the generator and
engine as a roost and nesting place for several years. The engine in
particular was loaded with pigeon droppings.
The northern area emergency generator work crew was assigned the task
of cleaning up the engine, changing oil and filters, installing new
batteries, and then trying to test run the engine. The engine started and
ran on the first try. It was a 900 KW generator set and would become our
largest replacement generator set set.
A windstorm with cyclone-like winds knocked down a large number of
power lines and supporting poles feeding power to a Company worker land
accommodations camp. The gas/oil plant where the personnel worked had
their own emergency generators.
When power was lost, the camp's emergency generator had started up and
tried to assume the load. The generator set was an older model and had not
been properly maintained.
All the control wires caught fire and turned into slag. The generator
set was 1000 KW, but out of service. The plant workers were dining on cold
sandwiches and warm water three times a day.
The only generator set available was the 900 KW set we had just test
ran four days before. The engine was still covered with pigeon droppings.
No matter. Plant personnel used a crane to pick up the generator set
after we had disconnected it and load it onto one of their trucks for
transport to the land camp site.
I had calculated the full load of the cooking facility with its large
ovens and freezers at just over 900 KW with everything going at full
usage. We disconnected the old generator and temporarily connected the
spare.
The generator was started and put on line immediately. Abdullah closed
the main switch and lo, there was light. The full load was put on the
generator one switch at a time.
The ammeter kept going up and up till all the switches were on and we
were running at full blast, just over 2000 amps at 240 volts AC. The camp
manager was happy and the cooks went to work preparing the noon meal for
the plant workers.
I assigned two men, one electrician and one mechanic, to watch the
generator set for each 12-hour shift. They would stay at the camp and eat
at the camp. Diesel fuel had to be trucked in every day until our Manager
finally got one of the trucks to be assigned to the camp, temporarily.
That generator set ran at full bore for ten days. Then, power was
finally restored. We left the generator set connected to the automatic
transfer switch while we repaired the old generator set controls and
engine.
The old generator set had been housed in a short shipping container.
The container was too small for the engine and not properly set up.
I worked with our new Area Engineer to design a simple storage building
for the generator set. The building could be constructed during the
generator set repair time and would be ready for the repaired set.
After the repaired set was installed and connected, the spare was
brought to our shop in Dhahran. The overhaul crew began repairs by
cleaning the pigeon droppings from the engine.
The repair crew leader wanted to show me something on the engine the
next day. A hole about the size of a dollar bill was found when the pigeon
droppings were cleaned off the engine air intake manifold. A diesel engine
driving a generator supplying 900 KW of power consumes an enormous amount
of air for combustion.
How the engine ran at full speed for ten days without pulling that
stuff into the engine and causing a blow-up is amazing. The intake
manifold on the engine was aluminum.
The pigeon droppings contained a chemical that attacked the aluminum
and then was compounded by the infrequent rain. It was pure luck for
everyone concerned that the engine held together.
The intake manifold was the only major part needing replacement on the
engine. The rest of the inspection and overhaul consisted of minor parts,
filters and gaskets.
We now had a 900 KW spare, a 250 KW spare, a 150 KW spare, a 90 KW
spare and a 50 KW spare. We could supply a temporary spare generator set
for nearly all our foreseeable needs.
Larry Bush
Also watch for more articles by Larry Bush at ...
http://www.Reliability-Consultant.com/Industrial_Articles.htm
About the Author: Larry Bush
has been an electrician for 47 years, and in maintenance management for 22
years. Download his new e-Book "Maintenance
Policy and Procedures Manual" !!
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