EMERGENCY GENERATOR SET
OVERHAUL
By Larry Bush

- Ref: detroit diesel generators, detroit diesel generator,
temporary generator, temporary power distribution, temporary power,
esg engineering, winding insulation class, cable damage curves,
winding insulation
Summary:
"Larry relates to issues with their Detroit
Diesel generator set for emergency temporary power distribution, in
the hope that the information might be helpful to the reader"
There were a number of incidents that occurred while maintaining the
Saudi Arabian Oil Company owned Emergency Supply Generators (ESG). I will
relate some of them in the hope that the information might be helpful to
the reader.
The Company had an Engineering Building with a computer center in
Dhahran that utilized a 1460 HP Detroit Diesel generator set for emergency
power. There was an emergency battery setup in the building that provided
emergency bridge-over power for up to ½ hour.
Nine months prior to our taking over responsibility from the company's
existing generator maintenance service providers, the Engineering Building
generator faulted out and was removed from service. A temporary
replacement emergency generator was rented from the local Detroit Diesel
vendor.
Five hundred MCM cables were temporarily installed and hooked up from
the generator to the connection points over 200 feet away. A replacement
part was ordered, "Rush", from the United States.
The maintenance unit waited and waited and waited. In the meantime,
costs for renting the replacement generator continued to mount. Renting a
1400 HP generator in Saudi Arabia was not inexpensive.
I learned that the long awaited part was due to arrive on site just two
days after the turnover date of the maintenance responsibility. I thought
that was rather fortuitous timing. We would be able to immediately repair
a money-consuming monster and look good doing it.
When the part was delivered, I saw that the part did not match the part
that was needed. The wrong part had been ordered or sent.
Fortunately, I had a contingency plan. The damaged part was a rectifier
that converted AC voltage to full wave DC voltage for the generator field
circuit.
I first visited the local Detroit Diesel vendor in the nearby city of
Al Khobar. I had visited their offices before and so knew just who to call
on. I took the part to them and asked if they had one or could rob the
rectifiers from a similar one to repair it.
LOCATING THE DETROIT DIESEL GENERATOR PART
The Parts Manager of the local Detroit Diesel vendor knew right where
to look. He searched his files to confirm the location and quickly
produced the rectifiers needed to repair the part. He then had his
company's shop make the repairs to the part. Problem solved.
IDENTIFYING THE ROOT CAUSE
Before we installed the part, I decided to examine the generator in
order to try to ascertain the reason for the failure of the part. I read
the manufacturer's manual on the generator and there in black and white
was the warning to refrain from carrying out a powered insulation test on
the generator circuit containing the field rectifiers or failure of the
rectifiers could result.
The generator was directly coupled to the engine shaft. The generator
shaft only had one bearing. The drive end of the shaft used the engine
bearing.
While checking the generator, I noticed a small amount of oil in the
bottom of the inside of the generator housing. We removed inspection
plates from the engine end of the generator and found the source of the
leak.
The engine drive-bearing seal had partially failed and oil was leaking
into the generator. The oil had gotten on and into the generator windings
and was affecting the insulation on the windings. The generator insulation
resistance to ground would need to be tested.
TESTING THE WINDING INSULATION
Abdullah and I re-read the generator manual to make certain we knew
what we were doing before testing the generator. We insured that all
delicate circuits were disconnected and then used a 1000-volt, hand megger
on the windings.
The windings were partially grounded and that was why they had been
meggered by the original unit that had burned out the rectifier circuit.
The generator would need to be thoroughly cleaned and then dipped in
liquid insulation and baked for a good repair. A new bearing would then be
installed on the engine and the seals would also be replaced.
At one time, our Company's heavy-duty repair shop had performed this
service. When I checked with them, they said they were only doing this
procedure in the Southern Area for oil field equipment.
For the repairs that I needed, they would send the generator out to a
contractor and I could expect the repaired generator back in six to nine
months. I told them to forget it. My unit could do it faster than that.
ENGINE AND GENERATOR OVERHAUL
I consulted with our crews and we decided to tackle the problems of an
in-place short overhaul of the 1460 HP diesel engine and
removal/reinstallation of the 4-ton generator.
I checked with our company Cranes and Rigging Unit and they said they
would move the generator from the ground to the back of a truck, that's
all. No other division or unit would tackle the job.
The generator set was located in the basement of the building. There
was a delivery ramp down to the basement floor level. A 5-ton traveling
hoist on a horizontal, I-beam track ran the length of the basement to the
delivery area loading dock.
All we had to do was uncouple the engine and generator, pick the
generator up, set it on a mobile platform, and then move the generator to
where the traveling hoist could pick it up. Then do the same procedure in
reverse to reinstall it.
I had to design, order the parts and have built the wheeled platform
sturdy enough to handle a four-ton load. While the platform was being
built, work continued at the generator set site.
Our overhaul/repair crew was ordering parts and laying out the required
work on the engine. They would need to replace the bearing with the bad
seal and check the other main shaft bearings.
They would also be opening and checking the pistons and heads. They
would not be replacing anything unless it was bad. We didn't anticipate
having to replace much more than gaskets and other easily replaceable
items.
MOVING THE 4 TON GENERATOR
In order to lift the generator after uncoupling, there had to be
attachment rings in place above the generator capable of handling more
than the full weight of the generator.
Fortunately, there were several rings already in place, probably
mounted during initial installation of the generator set. We only had to
add one more lifting ring. Three chain hoists each with a four ton
capacity would be used to lift and move the generator.
The generator had to be lifted and then moved partially out of the room
so the moving platform would have enough room to fit under the generator.
We were able to attach another chain hoist to a large welded beam to pull
the generator into position.
After depositing the generator on the hard-wheeled platform, it was
just a matter of pushing the generator to the traveling hoist. The load
was transferred to the hoist on the hoist track and the generator then was
moved to the loading dock and onto a truck bed.
The truck delivered the generator to the Detroit Diesel vendor shops
for prearranged repairs. The repairs were to be carried out on a rush
basis, overtime approved. This was still cheaper than the rental cost.
The generator repairs were to take three weeks, or less. Our repairs on
the engine would take about two weeks. We would then reinstall the
generator onto the engine and carry out our tests.
TEMPORARY GENERATOR SET PROBLEMS
We turned our attention to the temporary generator and cables lying on
the ground while work continued on the engine. I first wanted to test the
insulation resistance of the cables to ground.
This was an extremely important safety fact that I knew had been
neglected. The cables had been lying on the ground for so many months and
they had been dragged over the rough concrete and blacktop to different
locations.
The cables sometimes were in the way of vehicular access to and from
the loading dock. Some of the vehicles ran over the cables and,
apparently, caused damage to the insulation.
Abdullah brought the megger to the temporary generator site. We made
certain that the automatic start circuit for the engine was disabled and
we began to take insulation readings on the cables. Instantly, we had
extremely low readings on two sets of the cables for the A and B phases.
The cables were partially shorted together and grounded.
I had noticed during my time with the original crew that they started
the temporary generator by hand on a weekly basis, but did not close the
circuit breaker to feed power to the emergency circuit over the temporary
cables. I was told that the last time the system had functioned was 4
months earlier.
AT some point during the last four months, the cables had sustained
enough damage to render them an extreme safety hazard to personnel and the
temporary generator set. In addition, there had been no backup power for
the building emergency circuits.
We immediately tagged out the generator set, notified our division
superintendent and the building maintenance supervisor. Then, we began to
check the cables for the likely problem areas.
CABLE FAILURE ROOT CAUSE ANALYSIS
There were two 500 MCM cables for each of the three phases and more for
the ground connection. In the loading dock area, the cables had fallen or
been moved into a vehicle access area.
We figured this was a good place to start. The cables at this point
were lying on the blacktop all twisted around each other with tire marks
and scuffmarks.
The loading dock area was also the lowest point in the dock area and
housed the sump pit and pump for rainwater drainage and disposal. It
didn't rain often in Saudi Arabia, but when it did, we might get or 2 to 3
inches of rain in a one hour downpour.
If there was damage to the insulation, the water had probably
exacerbated the damage. Abdullah called over several of our work crews to
come to the loading dock to separate and try to repair the cables. The
cables were 500MCM and very heavy to handle.
After the cables were separated and tied up off the blacktop, we used
insulation splice kits to repair the damaged insulation on the cables. We
again meggered the cables after the kits had time to setup.
The repairs were successful and the cables meggered good. Now it was
time to start the engine and run a full-scale test.
TEMPORARY GENSET TEST
I contacted the building maintenance supervisor and he requested we
wait till most people had departed the building. It was already after my
crew's quitting time so I explained that we could not leave the place with
no emergency power.
He finally agreed to the test. The engine was started through a
simulated power loss feature in the building's plant control room.
The engine immediately came on line and supplied power to the automatic
transfer switch. The automatic transfer switch operated and transferred
the emergency building power load to the temporary emergency generator.
Success. Our repairs held up. The temporary generator performed as
required and all was well. The load transferred back automatically and the
generator ran for a preset cool down period and then shut down.
Abdullah and I showed the building maintenance supervisor what had
happened to the cables. The cables were only going to be required for
approximately 3 to 4 more weeks, but we wanted no more damage to the
cables.
CABLE DAMAGE PREVENTION
The supervisor got a crew to put up warning tape and cones to protect
the cables. I suggested he get stands and or sawhorses to place in front
of the cables with high-voltage, electrical warning signs to keep vehicles
and personnel away from the cables.
After two weeks of 24/7 days, the mini-overhaul of the engine was
complete. The generator repair facility had called for a time and place to
deliver the generator.
The generator arrived at the loading dock and was unloaded by our crew
using the traveling hoist and moved to the point closest to the generator
room. The generator was then put onto the mobile platform and pushed to
the room.
Installation of the generator proceeded smoothly. Coupling the
generator to the engine continued until finished. I wanted to be able to
test-run the generator set the next morning.
The engine had been started and run for about 4 hours after completion
of the repairs and before the generator had arrived. We knew the engine
would run, but did not know for certain that the generator/engine coupling
was accurate.
MAIN DIESEL GENERATOR SET TEST RUNS
Due to the one-bearing setup of the generator, a slight misalignment of
the generator shaft to the engine shaft could lead to a rapid,
catastrophic failure before the engine could be shut down. We were all
holding our breaths when the button was pressed and the engine roared into
life.
The overhaul mechanic crew leader wanted to run the engine and
generator set, unloaded, for four hours and then stop for a check of the
engine for overheating, bearing problems, and metal shavings in the oil.
If all was well, the engine would be started and run for 24 more hours
with a mechanic on duty at all times.
The generator set and testing was excellent. The temporary generator
and cables were disconnected and the original generator was connected to
the emergency system.
Transfer, stability, and power tests were performed on the generator
set that same day and the generator set was officially put back into
service in less than one month from the time we took over the new unit.
That was eight months less than the length of time the generator set had
been out of service under the old unit.
ANALYSIS and SUMMARY
The initial problem with the existing generator set failure was due to
the failure of the bearing seals on the rear bearing of the engine. This
bearing supported the engine and the generator shaft is bolted to the
engine shaft with another bearing on the opposite generator end.
The seal failure allowed lubricating oil from the bearing to seep into
the generator compartment. The oil dripped onto the generator windings and
eventually reduced the insulation resistance of the windings. This caused
an alarm to be tripped on the generator control panel.
The maintenance crew decided to use a hand powered, 1000 volt, DC
megger to test the insulation resistance windings to ground. The field
windings of this particular generator are powered through a full wave
rectifier setup to provide DC power to control the output of the
generator.
Using a 1000 Volt DC megger on this rectifier circuit would blow right
through the rectifiers and ruin them. This is what the maintenance crew
did when they checked the windings. There was no spare part on hand.
Without this part, the generator set was unusable
The generator set was built and delivered from the United States. The
part was ordered from the original dealer through the company's satellite
headquarters in Houston, Texas. Houston personnel bought and delivered all
the parts for Saudi Arabia from the United States.
I ordered the part through the local Detroit Diesel vendor after
getting permission to bypass the normal supply channels. This emergency
generator set was crucial to the oil company's operations and maintaining
and repairing it was a very high priority.
Root cause analysis was used to identify the actual problems and solve
them. The initial cause of the failure was the seal failure and the
subsequent seepage of oil into the generator compartment. There were a
number of breakdowns in good maintenance practices and I have listed them
following:
1) This oil seepage should have been identified by regularly scheduled
inspections and the problem corrected long before it damaged the generator
winding insulation.
2) The seals and bearing could have been replaced in one 24 hour period
with a huge savings in the actual costs.
3) The insulation resistance readings should only have been carried out
after reading and following the manufacturer's instructions listed in the
generator manual.
4) The spare parts should have been ordered through the local Saudi
Arabian vendor with an assurance that the right part would be available.
5) The temporary emergency generator should have been connected to
automatically start and assume the emergency load on main power failure.
6) The temporary emergency generator cables should have been placed in a
more protected location and tied up off the ground.
7) The temporary cables should have had protective signage and saw horses
placed around the cables.
8) The temporary cables should have been tested for grounds and shorts on
a regular basis.
Fortunately, there was no long term power outage to the buildings
served by the emergency generator during the four months that the cables
were grounded and shorted. Had the cables been powered during this period,
there could have been an electrical explosion and possible negative
consequences to personnel and equipment in the area.
Larry Bush
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About the Author: Larry Bush
has been an electrician for 47 years, and in maintenance management for 22
years. Download his new e-Book "Maintenance
Policy and Procedures Manual" !!
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